Kurze Zusammenfassung: GPS manuell ausgeschaltet, vom Wind abgetrieben.
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There were some dropouts on the RC-connection but very short, 2-4sec. The drone was controllable all the time.
At 21:24:10 there was a short GPS loss for 2sec. Reason unknown.
At 21:24:16 the GPS was switched off by switch (9) on ST24. Speed increases without any stick input up to ~6m/s. The drone keeps this speed with some variations due to stick inputs until the end. So, I think it is wind speed and it fairly looks like that.
21:25:50 landing looks like a normal manual landing, motors switched off by arming button (Trottle=0 for more than 3sec). At this point the best what the pilot could do - and success.
Here are the minor dropouts (red pins means received telemetry data):
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RC controls working, drone reacts as expected:
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The flight track:
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How the pilot moves towards the drone:
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br HE
PS: Kopf hoch, weitermachen. Alleine der Sound vom H920 ist geil.