- Joined
- Nov 29, 2017
- Messages
- 8
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- Age
- 61
I would like to have Yuneec look at any info on my ST-16 controller to help figure out why my drone ditched into a lake but I'm going to ask the experts here for their input first.
I was flying around videoing some dragon boat racing when I got ONE single low battery vibration from the controller so I flipped the switch to HOME. I was expecting to see the H rise up and fly back but instead what I got was a slow descent that kept going so I initiated a full throttle UP in hopes of keeping the H dry. What I got instead was a splash and the drone was lost.
This all happened with only ONE vibration which was the FIRST low battery warning. There are typically a few vibrations (I think) at this first warning then a bit of a delay then at the second low battery (critical) warning the H is supposed to lower the landing gear and land wherever it happens to be. I never got to the second warning (which I never wait for anyway because I usually already have the H on the ground) and the landing gear never lowered as it should when it lands on it's own.
After looking at the video of the crash on the controller it appears that the drone spiraled a little more than 360 degrees as it descended from about 50 feet into the lake. The drone was less than 300-400 feet from it's take off spot so returning after the first low battery warning should not have been a problem.
Please tell me the files needed so that someone can tell me what happened.
Thanks in advance!
I was flying around videoing some dragon boat racing when I got ONE single low battery vibration from the controller so I flipped the switch to HOME. I was expecting to see the H rise up and fly back but instead what I got was a slow descent that kept going so I initiated a full throttle UP in hopes of keeping the H dry. What I got instead was a splash and the drone was lost.
This all happened with only ONE vibration which was the FIRST low battery warning. There are typically a few vibrations (I think) at this first warning then a bit of a delay then at the second low battery (critical) warning the H is supposed to lower the landing gear and land wherever it happens to be. I never got to the second warning (which I never wait for anyway because I usually already have the H on the ground) and the landing gear never lowered as it should when it lands on it's own.
After looking at the video of the crash on the controller it appears that the drone spiraled a little more than 360 degrees as it descended from about 50 feet into the lake. The drone was less than 300-400 feet from it's take off spot so returning after the first low battery warning should not have been a problem.
Please tell me the files needed so that someone can tell me what happened.
Thanks in advance!